A functional update for the IV-11 DCF melody watch is available from gr-projects. It is a radio temperature transmitter. The special thing about it is, that the transmitter operating in the ISM band 433 MHz is equipped with a photovoltaic cell (solar cell). Depending on the version, a small rechargeable battery or a CR2032 button cell can be installed in the transmitter. The battery is thus supported by the solar cell in the sunlight or in the battery version it is charged during the day and then keeps the transmitter in operation over the dark time.
The assembly is easy. The kit consists of a transmitter and a receiver. The boards of transmitter and receiver are equipped with few components quickly. Here, however, some attention is required and you should read the documentation carefully, because due to the lower number of kits, the boards are manufactured without component imprint and solderstop.
The radio modules themselves are completely pre-assembled (SMD) and only need to be soldered into the corresponding circuit boards. Optionally, a trim potentiometer can be connected in parallel to the temperature sensor (NTC) for adjustment purposes. The transmitter, like the receiver, is installed in a small PVC housing. Here, except for a 3mm drill hole and possibly some silicone for the sealing of the solar cell (for operation outside the window sill) no further tools are needed.
To connect the receiver to the clock, make a few minor changes to the clock’s mainboard. First, the microcontroller is replaced – logically – because there is indeed a new program that then displays the temperature in the date line. A resistor is removed, one is added and a jumper can be swapped. The connection between the clock’s motherboard and the radio receiver is made with a piece of cable. Three lines are required (GND, + 5V and the data signal from the receiver controller to the clock controller). That’s it then already. The clock can go into operation. After a few seconds, the received temperature is displayed in the tube.
A video how to solder the circuit is available here:
Again and again it happens to me that a USB memory stick loses its function and is suddenly no longer recognized. Often the stick is still registered as a drive in the system, but it lacks the disk, or even the system reports that the stick is not formatted. And even though he just recently, full of important data, has worked in another computer. 🙂 (Here would now be the story with the backups or backup copies …). All these problems are mostly due to operator errors or mechanical problems. For example, an operator error may be that the stick is being pulled while one more writing is in progress. The stick is then de-energized during a process. And depending on whether the controller or flash memory can handle it, the stick will survive or not. Often, mechanical defects are the cause of breakdowns. So it may be that the solder joints between the connector and the board break, or get the connecting pins of the quartz or oscillators contact problems.
In this case, I got a miniature stick from extrememory, which does not want to give away its stored data. It is displayed in the system administration, but if you want to access it, the message “no data carrier found” comes. The attempt to format or partition over diskpart from the commandline did not work. Also various tools like “SDFormatter” or “USBstick_Formattool” failed. Even with Linux or on MAC systems, no success was achieved. So a stick for the barrel … But I thought, even if the stick in its small design rather not close to a mechanical defect – why not take a look anyway 🙂 And at 16GB I will not give up so fast.
So I tried to gently open the case by first removing the metal case of the USB connector.
That works quite well. After I wanted to take a closer look at the appearing small printed circuit board with its tracks, there suddenly appeared something familiar.
That looks like an SD card. More specifically, like a microSD card.
That’s the way it was. The USB stick is nothing more than a MicroSD card reader, in which such a card is installed. Using tweezers, the SD card could be levered out.
Apparently here again the problem is with the contacts, or contact springs between card and card reader. It is the cause of the problem, because the SD card worked fine in another card reader and all the data was available. It pays to invest in front of the garbage bin for a few minutes and to inspect the innards of the device.
At least one blog post per month to write I have set myself the goal, even if it is not always easy to implement this temporally. Anyone who has small children himself can perhaps imagine that. But in the evening and in between, I can collect material and edit it. -> it just takes everything much longer. This time I organized a Sony DAT recorder for retro audio. It is a Sony TCD-D3 from 1990-91, a so-called DAT Walkman.
DAT (Digital Audio Tape) is an audio magnetic tape recorded digitally. The recording format and the sound quality are essentially similar to those of the audio CD. The recording takes place on small cassettes, which were also used in the storage area in the EDP (DDS tapes). The DAT format was intended as the successor of the audio cassette, could not prevail in the broad market. It is also discussed here that the music industry did not want to see the format in the consumer world, as it was possible with the system to produce digital, lossless copies.
The technical structure of the cassette drive corresponds to that of a video recorder. The tape is pulled out of the cassette with loading arms and passed around a rotating head (DAT-R). The recording is done in helical scan. The copy, which I acquired this time as “defective”, was with the defect: Cassette shaft does not open, described. After dismantling, I noticed that I was not the first to look at the inside of the device after the factory. Someone was already messing around. All (tantalum) capacitors were soldered, the lead wires to the battery pole contacts were “pinched off” and the wires were missing. The Flexiprint, which connects the front panel to the mainboard, had a broken track when looked at closely.
The broken wire could be repaired by carefully scraping off the insulation and brazing a stranded wire. The capacitors I have all newly soldered and of course checked before. Here I noticed that some were not soldered properly and had a cold loosening at a pole or were not connected to the pad. The battery contacts were also provided with new wires. On the mainboard there is also a DC / DC converter, which makes the supply voltages for the logic and the audio components from the 9V input voltage. (5V +/- 7V). This converter is housed in a completely soldered tinplate box. Of course, nobody was inside and checked the Elkos inside. That was done quite quickly and the small box was overtaken. Now I was able to provisionally reassemble the boards and drive and put them into operation. As data carrier I used a DDS (storage) cassette. So tension on it and “Eject” pressed and lo and behold, the cassette compartment opens immediately. From my Handyaudioplayer as a music source, I made a trial recording. And what can I say, a wonderful sound quality!
The next issue to fix is more of a visual nature. These are the side casings, which are coated with a rubber coating and this begins to seem to change chemically and becomes sticky. So I washed this gum carefully with isopropanol and tried not to replace the white printed lettering with. That worked quite well. With acrylic clearcoat I then painted the parts.
After curing the clearcoat I was able to assemble everything again and start the final test. The following pictures show the inside of the TCD-D3.
The Sony RX100 digital still camera with its 20.2 megapixel EXMOR CMOS sensor impresses with its excellent image quality and compact design. The sensor size of one inch and the front Zeiss Vario Sonnar F1.8 lens are also responsible for the good image results. With 10x6cm and a thickness of 3.6cm, the camera is still suitable for pockets. (Although I would not recommend it). The 3.6x optical zoom lens is retracted when it is switched off and extended when in use.
But after some time and a number of in´s and outs of the optics, it may – or better – it will come to a situation where the optics refuse to serve. This manifests itself in different ways. Either nothing happens after switching on, the optics do not move and only the message (“Power Off and on again”) appears on the display, or the lens moves out a bit and then back in again. Now you could assume that the camera has mechanical damage, the sliding surfaces inside the optics are dirty, or something is bent or warped and jammed by a possible fall. But that’s usually not the case. In this case, the camera has never been subjected to strong mechanical, thermal, etc. stresses and there is still an error. If you do a little research on the Internet, you will find some repair tutorials where you try to clean with some paper strips between the slide rings of the optics etc. No reasonable information was found. So I have no choice but to look for the cause of the problem myself. And it was found quickly. After opening the device and slightly lifting the rear housing cover, the object suddenly extended again. If the lid was replaced, the problem was there again. So there had to be a contact error somewhere. In the following lines I present my way to a functioning camera:
After loosening the screws and removing the plastic base plate, the rear cover can be removed with the control panel and the monitor.
The Flexprint for the screen and the one for the control unit can be released, the small speaker can simply be hung up. Now the battery can be inserted and the camera can be switched on again. In this case the lens opened and extended again correctly. So it’s really a contact problem. But where? I tried to put light pressure on the Flexiprint, which supplies the mechanical part of the optics. (Not the one that leads from the sensor to the mainboard.) With this slight pressure on the Flexprint, the device was switched on again and lo and behold -> hit. The optics didn’t move. That could also be understood. So this Flexprint seems to have a line break at the kinks. Apparently, this print is mechanically stressed due to the construction and retraction of the lens and thus yields and breaks at some point. (Perhaps also planned obsolescence). Anyway, I looked for a replacement on the net, found it and after a week of waiting the new Flexiprint was already delivered.
The new print for the optics is sold without any components. This means that from here a little experience in handling soldering tools, SMD components and flexible circuit boards is required.
The optics must be exposed and removed. To do this, the mainboard must be detached. (three screws in total). Then carefully remove the black film from the back of the optics. (Be careful with all flexible cables) Once the film is off, the flexprint to the sensor can be unplugged.
Next, the motor unit is released and the motor is separated from the lens housing.
There are some components on the print, such as plug connections and small fork light barriers, which are installed in the lens (lens position) and in the motor unit (two pieces as incremental encoders and for determining the direction of rotation). These are held in place with small metal brackets and must be released before removing the lens unit.
The lens, drive unit and mainboard are removed. All plug connections between the optics and the drive motor must be disconnected.
The motor unit can now be separated from the lens. The Flexiprint is attached to the lens housing with tape and small hooks. These have to be solved.
Now disassembly of the motor unit continues. As previously mentioned, there are two fork light barriers in the plastic housing of the motor gearbox, which are also held in place with a clamp. This can simply be clipped out. To complete the removal, the motor must be unsoldered. Now the Flexiprint is free and the delicate step can begin.
The small SMD connectors must be unsoldered from the old print and reattached to the new print. This work requires cleanest hand towels, as the small plastic housings can be easily destroyed when unsoldering. I recommend here to heat the print only from the bottom, and then lift the plug off with tweezers. Otherwise you run the risk of deforming the plastic of the connector too much heat. If this is successful, the plugs can be soldered onto the new Flexprint.
The same work is also to be done with the fork light barriers. Then only the contacts of the motor have to be soldered to the designated positions in the flex board.
If that worked, the assembly can be done in reverse order. When bending the flex board into the correct position, you can orient yourself on the old board. Then the installation should not be a problem. A function test should be carried out before attaching the rear wall of the camera (rear cover). The lens must extend and retract without a monitor or control panel. If that also works, then it can be finalized. In my case, the repair was successful. Let’s see how long it takes for another conductor to break in the flexible PCB …
A new member of the collection of old multimedia devices is the Panasonic AG-6400. The AG-6400 is a (semi) professional video recorder from the 80s. The device records on VHS magnetic tapes and also reproduces this standard. It is portable and was the recorder for the video cameras of that time. It draws its energy from 12V NP1 batteries and can provide approx. 27W for the camera connected to it. That was about the power requirement of a 3-tube camera.
This device, too, had gotten some traces of time that largely restricted its function. Simply said – it was broken. This defect manifested itself in a stuck capstan shaft . At first I thought the shaft was ‘seized’ due to corrosion, but the reason was completely different. Interestingly, a ball bearing had been pressed out of its press fit, so that the flywheel attached to the shaft touched the bobbin of the capstan motor. The magnets in the flywheel held it in place. This error could be easily and quickly remedied by pushing back the ball bearing and then fixing it.
After the mechanical fault was repaired and a first function test, a fault in the 5V power supply was still to be found on the power board. This was expressed by a failure to start all drives. Here, an IC fuse was defective in the switching converter. This was triggered by a defective Schottky diode in the buck converter circuit. This bug was also quickly solved. And after checking and adjusting the operating voltages according to the setpoints in the service manual, the drive did its job again. I was even amazed at the excellent image quality that the device could reproduce. Due to its compact dimensions, I can even use the AG6400 to digitize old VHS tapes in the future.
In the data sheets and advertising for the AG-6400, the manufacturer has advertised some features and functions as follows:
High quality image reproduction
The tape speed corresponds to the VHS standard with a video track width of 49µm. Several technologies for clear and detailed image reproduction are combined in the device.
A four-channel system consisting of two ‘normal’ audio channels with Dolby noise reduction and two ‘HD-Sound’ channels allow you to enjoy high quality recordings. A 3.5mm headphone jack and two 6.3mm microphone jacks for separate feeding of both channels, including separate control with VU meters, complete the range of audio options.
Time Code record and playback For control in linear editing systems, the recorder enables the recording of external EBU timecode signals on channel 2 of the longitudinal track.
A connection for an external camera with a maximum power consumption of up to 27W is also available. Cameras with 3-tube Vidicon system can be connected here.
A diagram with the connection options is shown in the following picture:
Occasionally I browse flea market websites for vintage and retro devices from the 70s, 80s and 90s. If an absolute bargain is in sight, then I strike and sacrifice a few euros. This time I found a whole box of Sony portable media players. The whole thing just cost me the equivalent of a pack of Cafe. However, the state of the devices in terms of function is also unknown. A particularly beautiful piece (yes – that’s always in the eye of the beholder) from this box is the Videowalkman GV-8E from Sony. This is a portable, analog video player / recorder that has a VHF / UHF television tuner and an LCD monitor integrated in one device. While that may not be anything exciting today, the GV8E was a very nice and expensive piece of technology when it was launched in 1988. So the portable lands on my table and gets its 6V DC supply from the power supply. The disillusionment comes as quickly as the initial euphoria. The device shows no function despite the power supply being upright. It does not react to any key press, no LED lights up. (Somehow I was expecting this or something similar)
But the ambition is too great not to look inside the device and to look for the problem. I quickly started disassembling and roughly dividing the device into its components. The service documents can be found online, which are very helpful here.
After examining the block diagram of the entire system, the start of the troubleshooting was the DC / DC converter board. This board, covered by a shield plate, produces all the voltages required for the supply of the individual components from the 6V input voltage. A measurement on the test pins on the board showed that some voltages were missing. So there must be a problem here.
After removing the shield plate and inspecting the components, I noticed a defective 1.6A fuse (F103). This fuse protects the primary circuit of the switching converter. It can be seen from the plan that transistor Q114 was low-resistance and thus caused the fuse to trip.
The transistor is a 2SB1121 bipolar PNP transistor. Of course I didn’t have that in my collection. So thinned the component boxes for a suitable replacement …
Then I found a PBSS5250Z, which has a slightly larger housing, but should do its job in the circuit.
Due to the larger design and the limited space available, I could only solder the replacement transistor upright.
Now a new fuse is still missing in the board. After installing and checking the other components in the affected circuits, the next function test was started. All boards electrically connected again and 6V connected to the battery terminals – and look – the Powersupply board starts up and the voltages are there. Now the GV8E can be switched on again with the power button, the LED also lights up and a quiet noise can be heard from the loudspeaker. However, none of the drive motors are running and the LCD monitor remains dark. The LED lights up briefly when the “Ejekt” button is pressed, but the motor responsible for ejecting the cassette compartment does not start. That means -> continue searching for errors. First of all I will take a look at the LCD monitor. It is quickly removed and dismantled. All the less pleasing is the condition of the board. Here the “decaying” electrolytic capacitors raged with their “body fluids”. (Of course this means the electrolytes)
The liquid electrolytes of the electrolytic capacitors have leaked over the years and have attacked the conductor tracks and also the solder joints. Sometimes it is so bad that small components, such as SMD transistors and resistors, fall off the board as soon as they are touched. At the latest now it is absolutely necessary to have the circuit diagram of the device at hand. Otherwise it will be difficult afterwards to correctly refill the missing parts. But first the old electrolytic capacitors had to be removed.
With PCB cleaner I was able to remove the remains of the electrolytes and only then could I see the damage to the circuit board. Corroded areas had to be sanded with a glass brush and burned components had to be replaced. After cleaning again, the new capacitors (this time ceramic multilayer capacitors instead of the electrolytic capacitors) have found their place.
After this procedure the time had come. The next function test started. After reconnecting all plug connections and the power supply, there were further signs of life. The backlight (CCFL) started again and in the upper left corner it was “00:00” to see the flashing clock of the on-screen display … Unfortunately, that was all. The OSD display was very blurry and the rest of the picture was white. The brightness controls did not respond. So the board had to be examined “big”.
The board of the LCD monitor still had many broken conductor tracks, which had to be laboriously repaired with individual strands and enamelled copper wire. There were also some SMD components (resistors and transistors) so corroded at their connections that only an exchange helped. The result looks a bit wild, but another function test was finally positive.
After I reassembled the monitor, I went to the drive. Here, too, I first checked or renewed all SMD electrolytic capacitors, as ALL of them had really leaked out. Fortunately, the circuit boards here were not so severely etched and can be easily cleaned. Then the function test came. And unfortunately there were still problems here. There was no cassette ejection and no reaction from any of the drives. After studying the service manual and measuring many supply voltages, I was able to identify a processor as a source of errors. It is a SONY CXP80116.
This chip controls all drives, leds, queries sensors, etc. It is also responsible for ejecting the cassette compartment. It controls a driver IC (bridge) via pins 20 and 21, which in turn supplies the charging motor. And exactly the two outputs remained at 0V. When the “Eject” button was pressed, only a few millivolts were measured instead of the 5V. So at first there was a suspicion that the driver IC has an error and is pulling down the outputs of the controller. So the outputs from the controller to the motor driver were separated and 5V directly connected to the motor driver input – and lo and behold, the loading motor was activated. So the problem is with the 80116. After some back and forth I was able to find one of these and exchanged it. Another test pleased me, because the cassette could be loaded again and the head drum started.
And the next problem already appeared. One of the two loading arms only drove half off and then got stuck. That means I also have to disassemble the mechanics of the drive. Said and done. Fortunately, it was only a small bolt that holds a drive lever. This had loosened and slipped out. So the problem was quickly resolved. Now I was finally able to do a function test again. And this time everything worked. The cassette was loaded, the head disk started, the tape was threaded and finally it could be played. After I had tested all functions, the GV-8E can be reassembled. Now he can go to the showcase as a “museum piece”;)
Technical data of the GV-8E:
Video recording System: Rotierendes Zweikopf-Helical-Scan-FM System
Audio recording System: Rotierender Kopf, FM System
The bench multimeter from Keithley is an old companion in the field of measuring instruments. The types of the 2000 series are predominantly used in our laboratories. They are available in different equipment variants with regard to the interfaces to the outside world. Here GBIP bus is of course a standard, as is RS232. The newer devices now have a LAN interface with which communication via the Internet protocol is possible. Each of these interfaces can be used to communicate with the device using “Standard Commands for Programmable Instruments” (SCPI). In this example I will control the Keithley 2000 via Matlab and read out measured values cyclically over a longer period of time, save them in Matlab and finally output them in a plot – virtually configure a simple data logger. The purpose of this setup is to record the voltage curve (or current) of a rechargeable battery or battery of a low-energy device.
In this example I will use the serial data transmission via the classic RS232 interface, as this is completely sufficient for my application. In addition, I can save myself the installation of the driver packages for the GPIP-USB interface. 🙂 Since many of the current computers and laptops no longer have any RS232 ports, a USB-RS232 adapter (e.g. FTDI232 etc.) is required.
Once the connection between the multimeter and the computer has been established, communication can take place via a Matlabscript, as in this example. The Keithley only needs to be told that it should “talk” over the serial interface. The following code snippets show how you can easily read out data via SCPI:
serialObject = instrfind('Type', 'serial', 'Port', 'COM26', 'Tag', '');
%serialPort = 'COM23';
%serialObject = serial(serialPort,'BaudRate',9600, 'DataBits',8);
serialObject = serial('COM26','BaudRate',57600, 'DataBits',8);
serialObject = serialObject(1)
% Sourcemeter 2000 setup
time = now;
voltage = 0;
figureinstanz = figure('NumberTitle','off',...
'Color',[0 0 0],'Visible','off');
plotinstanz = plot(voltage,time,'Color','red');
%% Messzeit und evtl Messintervall
stoptime = 10; %60 seconds
timeInterval = 1; % brauch' ma jetzt nicht
% Messgeraet einstellen
fprintf(serialObject,':SOUR:FUNC:MODE CURR'); % current source selection.
fprintf(serialObject,':SOUR:CURR:MODE FIXED'); % changes voltage mode to fixed
fprintf(serialObject,':SOUR:CURR:LEV 0'); % sets current to 0
% %fprintf(serialObject,':TRAC:COUN 1');
% %fprintf(serialObject,':TRAC:FEED:CONT NEV');
% fprintf(serialObject,':TRAC:POIN 10');
% fprintf(serialObject,'TRAC:FEED:CONT NECT');
% fprintf(serialObject,'TRIG:COUN 10');
% fprintf(serialObject,':OUTP ON');
%% Daten abholen
count = 1; voltage(1)=4
% while time<=stoptime
% fprintf(serialObject,':TRAC:FEED SENS');
voltage(count) = fscanf(serialObject,'%f');
time(count) = toc;
count = count +1;
grid on; hold on;
xlabel('Zeit [s]'); ylabel('Batteriespannung [V]')
title('Spannungsverlauf Batterie 3V Lithium (2032 mit Modul) im default mode');
% fprintf(serialObject,':OUTP OFF');
%% Put the instrument in local mode
The following plot shows what such a data log looks like. Here, the voltage curve of a nearly discharged battery is recorded over time until the consumer is switched off.
In this post I would like to devote myself to something else. It’s not about retro technology, it’s about a little thing that makes working in the office/lab easier. One of the many measuring devices I deal with is an old Agilent LCR meter. As is known, the LCR Meter 4297A can be used to measure the inductance, capacitance, etc. of electrical components and generally of structures which are assigned to the electronics / electrical engineering sector. Roughly speaking, the 4297A actually only measures current / voltage, the phase relationship between the two and the energy direction. And at a certain frequency. All parameters such as L, C, R, X, Y, Q, PHI, … are then mathematically calculated and output from these parameters. The frequency here can be set from 1MHz to 3GHz (in 100kHz steps). Ideally, the measuring device can measure not only in one frequency point, but also in many. By “many” is meant here that the measuring device can generate frequency tables with 32 entries. There are eight of these tables. This makes it possible to display the course of a measured variable in the form of a curve. However, this is quite cumbersome. The contents of the tables must be exported and saved manually (as “csv” files) table by table. This means that each table must be selected individually. Then select the “Export List View” dialog – then specify a storage path and file name. Only now are the first 32 records exported. This process must be repeated eight times in total. It is saved on a 3.5 inch floppy disc – the only available medium. You could also hang the 4297A optiona on a LAN and set up file sharing. However, manual export is not spared. The .csv files can now be opened on a “normal” computer. They must then be put together manually in postprocessing. Only now can a diagram be made from the data. Here Matlab from Matworks is a good tool, which is often used in our laboratories as part of training.
To simplify this cumbersome process considerably, I created a small script that communicates with the measuring device using the SCPI commands (Standard Commands for Programmable Instruments). That means: The measuring device is connected to a PC via a GPIB-USB controller. A Matworks Matlab installation including the required toolboxes is located on the PC. The Matlab script should now simply switch through the tables in sequence and read out the contents of the individual parameters and save them in an array. The content of the arrays is then displayed directly in a plot. However, this method only uses the contents of the tables. It would of course also be possible to set any desired frequency directly in a loop using the script, read out the measured values, select the next frequency, etc. This would max. Total 29990 points over the entire frequency range. The eight tables, each with 32 points, only allow 256 points. For now, however, that is sufficient and also much faster.
The example shows the impedance curve (Z curve) of a 50 Ohm transmission line. The end of the line is terminated with a 50 ohm resistor. The frequency range is 1MHz to 3 GHz. The situation is different if the line is open or closed briefly. The electromagnetic wave is then not converted into thermal energy at the end of the line, as in the “matched” system, but is reflected back into the system.
The following very simple Matlabscript enables the reading of the measuring device parameters. The script serves as an example of how to get the measurement data quickly. The programming manual of the manufacturer of the LCR meter lists all SCPI commandos and plenty of examples with which you can communicate with the measuring device.
%auslesen der agilent LCR Keule 4287A
%gekodet von ingmar bihlo Ende November 2017
%anschluss über gpib ni adapter
%LCR gpip adresse: 5
%vorarbeiten an LCR Keule
% Es müssen 8 Tabellen mit je 32 Punkten definiert sein
% (power und average ist egal, wird nicht ausgelesen)
% die CALibration muss gemacht worden sein
% unter "measurement parameters" muessen vier parameter definiert sein
% zb. Z, qhi, R, L, etc... diese sind dann in den variablen param1 bis 4
% gpib interface oeffnen und identifier lesen
g = gpib('ni', 0, 5);
g.InputBufferSize = 100000; % Set the buffer size
idn = fscanf(g);
num1all=0; % initialisieren der variablen für den summenvector
%read list parameters (frequency points)
clear listchat; clear fpoint;
%analyze list content
fprintf(g, strcat(':SOUR:LIST:TABL 0',num2str(i)));
pause(1); %pause 1s zum umschalten der tabelle
fprintf(g, ':DATA:FDAT1?'); %parameter 1 anfragen
par1=fscanf(g); %parameter 1 holen
string1=strsplit(par1,','); %parameter 1 string nach komma zerlegen
%num1=[cellfun(@str2num, string1(:,1:end))] %parameter 1 strings in dec konvertieren
num1all=[num1all,num1]; %parameter1 aktuell mit parameter1 aus vorherigem durchlauf concentenaten
%read list parameters (frequency points)
list=listraw(:,2:end); %von pos2 das feld schreiben (an pos ist die anzahl der zeilen)
freq=[freq,list(c)]; %von jedem 3. wert aus list ein neues array bilden
clear listchat; clear fpoint;
% Cell array richtig uma drahn
param1 = [y1 x1];
param2 = [y2 x2];
param3 = [y3 x3];
param4 = [y4 x4];
%uerberflüssige variablen loeschen
clear c; clear i; clear list; %clear freq;
clear par1;clear par2;clear par3;clear par4;
clear string1;clear string2;clear string3;clear string4;
clear num1all;clear num2all;clear num3all;clear num4all;
%plotten der ergebnisse
grid on; hold on;
xlabel('Frequency [Hz]'); ylabel('Measurement Parameter1 |Z| [Ohm]');
title('Agilent LCR Keule');
grid on; hold on;
xlabel('Frequency'); ylabel('Measurement Parameter2');
title('Agilent LCR Keule');
grid on; hold on;
xlabel('Frequency'); ylabel('Measurement Parameter3');
title('Agilent LCR Keule');
grid on; hold on;
xlabel('Frequency'); ylabel('Measurement Parameter4');
title('Agilent LCR Keule');
The Sony TC-150 is the newest, old member of the collection. Once again purchased as a defect device, this baby found a place in the workshop. After a quick inspection, it was immediately clear that the ravages of time were gnawing and, as is often the case, the drive belts became brittle or decomposed. Otherwise, the device is in perfect condition, hardly any scratches and damage to the case. The battery compartment was also clean. There are four belts of different lengths in the device.
Suitable replacement belts can be obtained, for example, from a large electronics store that is represented in Austria by six megastores. You will quickly find what you are looking for under the name “drive belt range” and “1.1mm edge length”. Replacing the straps is less quick. Here you should take at least half an hour and carefully take the drive apart.
The main circuit board must be removed in order to access the pulleys or to be able to unscrew them further. However, this is only possible if some lines are unsoldered. Only then you can fold up the board. Once that’s done, you can unscrew the retaining plates above the pulleys. They form the backing of the flywheels (capstan shaft). On this occasion, it is advisable to check the capstan shaft for dirt (due to belt wear) and damage, or it should be cleaned. The pressure roller must not be neglected either. In this model, both were in great condition. The pinch roller was neither glazed and brittle, nor contaminated with tape wear or shrinked. So I could put on the new straps. The main belt from the engine is put on with a rotation of 90 °. Here you should note the installation position of the old belt, if it still exists, or at least do a short test run after fitting the new belt.
If everything turns again (and especially in the right direction) then the assembly can be done. Solder the wires again, screw the circuit board and the repair is done. To have this man a test cassette, here are some parameters, such as tape speed or the tracking of the tape head, which are given and adjusted if necessary.
Technical data of the SONY TC-150:
Type: TC-150 (Europa) bzw. BT-50 USA
year of production: ca. 1977 – 1982 (according to various sources)
Modell kind: portable Cassette Corder
tape speed: 4.8cm/s
heads: 1 recording-/playback head
1 earase head (Permanentmagnet)
semiconductors: 8 tranistors, 5 diodes, 2IC´s, 1 FET
Power : Outputpower: max 360mW
Powerconsumption : max 9W
Supplyvoltage: battery 4×1.5V AA, or accupack BP28
12V Caradapter bzw. 6V 4W wallplug
operationtime: 2.5h at continous recording
Speaker: dynamic 5cm Lautsprecher
Abmessungen: 174 x 29.5 x 113 mm (BxHxT)
weight: ca. 769g
This beautiful, small, new piece of technology from the eighties has been added to my collection. It is a small tube radio receiver with radio part called CIRT-2097T from the manufacturer Broksonic (according to Internet research it is an US company). The device I received with the attribute “defective” quite cheap on a flea market platform. So I thought, the risk can be taken and risk a repair attempt. What great things can not be broken – if it’s not just the picture tube.
After a short functional test with the plug-in power supply, it soon became clear that nothing was working. No picture – no sound, no nothing. Since the device also has a battery compartment, I next wanted to try to feed the power via the battery terminals to see if there may already be a problem. And there it was already – the problem. The battery cover was almost impossible to get off, it held as glued. After some back and forth, I got the lid but then non-destructive and it revealed the cause of “jamming” or better “gluing”. There were still batteries in the battery compartment (probably for 20 or more years). They were in a bad condition, totally corroded and leaked. In part, the outer coat of the cell was corroded and no longer available. Oh dear – I thought, hopefully the leaked dielectric did not move inside the unit and did damage there. There was nothing left for me to do but to disassemble and check everything. And then the evil manifested itself:
About a quarter of the TV board had come in contact with the battery fluid. And the stuff has done a great job, etched away almost all the traces and leads from components.
So I first tried with PCB cleaner to remove all the crystals and the rest of the battery juice to get a closer look at the damage. A few random measurements with the ohmmeter quickly showed that many traces were severed. So it did not help, the tracks had to be uncovered. Only then would a reasonable repair possible.
With a rotating brass wire brush, I then began to remove the etched areas, remove the remains of the solder resist and expose the copper traces.
After the rough preliminary work had the glass brush ran. Only with that it was possible to remove all paint and corrosion residues and finally expose the traces. A tedious job …
… but finally it was possible to uncover and repair all damaged areas. Some resistors and capacitors also had to be renewed because their leads were also in poor condition.
After the repair, a bump test could then be carried out – lo and behold, there was no further error and the device was working properly again. So I was able to protect the repaired area of the board with solder varnish from renewed corrosion and reassemble the device.
Finally, here is an overview of the technical data:
vendor: Broksonic (US-Firma New York)
year of production: ca. 1982
model: TV+FM Empfänger portable
screensize: 2 Zoll SW Bildröhre
bands: AM, FM, SW (Radio), VHFI,VHFIII,UHF (TV)
VHF Kanal 2-13(US), 2-12 (E)
UHF Kanal 14-83(US),21-69(E)
supply: battery or accu, AC with adaper
supplyvoltage: accu 6V, battery 6×1.5V AA
speaker: dynamic 16 Ohms speaker
dimensions: 150x53x202 mm (BxHxT)
weight: ca 1.1kg
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